In this study the applicability of the microsieve technology together with coagulation and flocculation for advanced phosphorus removal was investigated. A pilot unit including a microsieve with 10 µm mesh size is operated continuously with secondary effluent. By applying a pretreatment of 0.036 – 0.179 mmol/L coagulant and 2 mg/L cationic polymer total phosphorus values below 100 µg/L were easily achieved. Values below 50 µg/L were possible at high metal dosing, but the higher suspended solid load reduced the capacity of the pilot unit. Coagulation with polyalumium chloride (PACl) produced better effluent quality compared to FeCl3 as less suspended solids and less residual coagulant were found in the microsieve effluent. Also the transmission of UV radiation through the water is improved by using PACl. The amount of backwash water was very low (< 3 %). In total, if combined with UV disinfection, microsieving with chemical pretreatment is a viable option for high quality effluent polishing.
In this study the applicability of the microsieve technology together with coagulation and flocculation for advanced phosphorus removal was investigated. A pilot unit including a microsieve with 10 µm mesh size is operated continuously with secondary effluent. By applying a pretreatment of 0.036 – 0.179 mmol/L coagulant and 2 mg/L cationic polymer total phosphorus values below 100 µg/L were easily achieved. Values below 50 µg/L were possible at high metal dosing, but the higher suspended solid load reduced the capacity of the pilot unit. Coagulation with polyalumium chloride (PACl) produced better effluent quality compared to FeCl3 as less suspended solids and less residual coagulant were found in the microsieve effluent. Also the transmission of UV radiation through the water is improved by using PACl. The amount of backwash water was very low (< 3 %). In total, if combined with UV disinfection, microsieving with chemical pretreatment is a viable option for high quality effluent polishing.
Numerous papers have been published studying the causes of fouling in membrane bioreactors (MBRs) and searching for a universal fouling indicator. Unfortunately, as these studies were performed using various set-ups and operating conditions (different membranes, sludge retention time (SRT), hydraulic conditions and diverse feed wastewaters, etc.), the results in terms of fouling rates and the infl uence of individual parameters rarely match up. In order to obtain a signifi cant database of comparable results from different plants, an intensive monitoring campaign of four MBR systems started in 2007 in Berlin. In these units, 14 parameters were monitored on a weekly basis over 10 months to characterise the mixed liquor and the corresponding permeability, including the novel parameter transparent exopolymer particles (TEP), which represent a specially sticky fraction of the extracellular polymeric substances (EPS). By performing statistical analyses it was demonstrated that there is no unique fouling indicator, and origins of fouling must be searched in the combination of several parameters using multivariable analysis. Applying a multiple regression the critical fl ux values could be correlated with four parameters (temperature, nitrate, bound and soluble TEP) measured in the activated sludge for 95% of the data.
Within the 3.5 year ENREM project (Enhanced Nutrient REmoval in Membranebioreactors) in Berlin-Margaretenhöhe a novel and patented process was investigated to demonstrate the feasibility of a semi-decentralised solution reaching high effluent requirements set by the water authority of Berlin. This novel process could be a solution for suburban areas of Berlin which are not connected to central sewer system. The biological process combines enhanced biological phosphorus removal (EBPR) with post denitrification in MBR technology without dosing of any carbon sources. The process configuration of this demonstration plant enables advanced wastewater nutrients removal (C, P and N) and could be a promising option for wastewater treatment wherever high effluent qualities are required. A second prototype MBR system was operated in parallel, applying a different biological process, e.g. without biological phosphorus removal, enabling a comparison of these different technological approaches. The demonstration plant showed high elimination rates for COD (>95%), phosphorus (>99%) and nitrogen (up to 98%) when operated within the appropriate range of design conditions. The operational experience within the first years showed that there is a possibility for process stabilisation by changing the ratio of the process steps. For this reason the volume of the anoxic zone was enlarged by reducing the aerobic volume in Feb 2008. The positive effects could be seen on the basis of the effluent concentrations after a short period of adaptation. The membrane filtration performance was very reliable with a new cleaning strategy: Two membranes were operated alternating with an operational flux of 15 – 20 L/m²/h and a maintenance cleaning with low chemical concentration. Different cleaning agents were used in order to evaluate the cleaning efficiencies. An economical evaluation of the demonstration plant was performed in comparison to the existing wastewater treatment costs of app. 7 €/m3 by trucking away and the prototype MBR plant. Operated on the same site, the two MBR systems were used to calculate the actual costs, in relation to the effluent quality, and to perform a scale-up up to 5000 pe considering four different effluent quality classes. The results showed that the ENREM process applied in the demonstration plant is economically an alternative for plant sizes of 5000 pe and larger. For plant sizes smaller than 5000 pe, the prototype MBR system equipped with precipitation and a downstream adsorption filter for enhanced phosphorus removal proofed to be the more viable solution.
Three different methods for fi ltration characterization in Membrane Bioreactor (MBR) systems were compared. These were the Delft Filtration Characterization Method (DFCm), the Berlin Filtration Method (BFM) and an ex situ side-stream fi ltration test cell for the determination of the critical fl ux. The ex situ fi ltration test cell and the DFCm fi lter activated sludge from a tank, while the BFM works in situ with a test cell directly submerged into the biological tank at similar operational conditions to a typical MBR plant. The mixed liquor of four different MBR units was characterised several times with the three fi ltration methods. The three tested methods seemed to agree in the classifi cation of the tested mixed liquors in terms of fi lterability except for one of the tested activated sludges. Additionally, three critical fl ux protocols were studied using the BFM fi ltration test cell. The fi rst consisted in the classical fl ux-step method, the second included relaxation between fi ltration steps and in the third protocol, 2 min fi ltration at a fi xed fl ux were performed before every fi ltration step. The last protocol was selected as the most representative of full scale MBR operation and the most interesting one for giving valuable information about the irreversibility of the fouling.
Due to their compact design and their high quality and reliable treatment, package or containerised membrane bioreactor (MBR) units are used for decentralised and semi-decentralised wastewater treatment plants. The operational availability, performance and economical viability of these MBR systems depend on the fi ltration performance of the membrane modules. Current chemical cleaning strategies of MBR modules, based on regular (weekly) maintenance cleanings and/or occasional (quarterly to biannual) intensive cleanings proved not to be adapted to semi-central MBR applications (100 up to 1000 p.e.): regular maintenance cleanings require automation and lead to too much care and personnel requirement. Occasional intensive cleanings increase the operational risk of membrane fouling and low cleaning recovery. In addition, semi-central MBR applications are often designed with at least two redundant fi ltration lines. An alternative chemical cleaning strategy was therefore proposed, implemented and assessed in a containerised MBR unit serving a population of about 250 p.e.: at a given time, only one fi ltration line is in operation while the other one soaks in a low-grade chemical solution. The modules are switched alternately on a monthly basis. To identify a cleaning strategy and an agent showing a good recovery, one of the modules was cleaned with H2O2, while the other was cleaned with NaOCl. A cleaning step with citric acid is added when necessary. These cleanings were tested over 16 months with the goal to minimise maintenance effort and chemicals used.